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- It's been about two years since I last posted this, so...
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- Excerpts from the NTSB accident report on the Chicago O'Hare crash:
-
- Synopsis:
-
- About 1504 CDT, May 25, 1979, American Airlines Flight 191, a McDonnell-Douglas
- DC-10-10 aircraft, crashed into an open field just short of a trailer park about
- 4600' northwest of the departure end of runway 32R at Chicago-O'Hare Internat-
- ional Airport, Illinois.
-
- Flight 191 was taking off from Runway 32R. The weather was clear and the vis-
- ibility was 15 miles. During the takeoff rotation, the left engine and pylon
- assembly and about 3 ft of the leading edge of the left wing separated from
- the aircraft and fell to the runway. Flight 191 continued to climb to about
- 325' above the ground and then began to roll to the left. The aircraft con-
- tinued to roll to the left until the wings were past the vertical position,
- and during the roll, the aircraft's nose pitched down below the horizon.
-
- Flight 191 crashed into the open field and the wreckage scattered into an
- adjacent trailer park. The aircraft was destroyed in the crash and subsequent
- fire. Two hundred and seventy-one persons on board Flight 191 were killed;
- two persons on the ground were killed, and two others were injured. An old
- aircraft hangar, several automobiles, and a mobile home were destroyed.
-
- The National Transportation Safety Board determines that the probable cause
- of this accident was the asymmetrical stall and the ensuing roll of the air-
- craft because of the uncommanded retraction of the left wing outboard leading
- edge slats and the loss of stall warning and slat disagreement indication sys-
- tems resulting from maintenance-induced damage leading to the separation of the
- No. 1 engine and pylon assembly at a critical point during takeoff. The sep-
- aration resulted from damage by improper maintenance procedures which led to
- failure of the pylon structure.
-
- Contributing to the cause of the accident were the vulnerability of the design
- of the pylon attach points to maintenance damage; the vulnerability of the
- design of the leading edge slat system to the damage which produced asymmetry;
- deficiencies in Federal Aviation Administration surveillance and reporting sys-
- tems which failed to detect and prevent the use of improper maintenance proced-
- ures; deficiencies in the practices and communications among the operators,
- the manufacturer, and the FAA which failed to determine and disseminate the
- particulars during previous maintenance damage incidents; and the intolerance
- of prescribed operational procedures to this unique emergency.
-
-
-
- Findings (p. 67)
-
- 1. The engine and pylon assembly separated either at or immediately after
- takeoff. The flightcrew was committed to continue the takeoff.
-
- 2. The aft end of the pylon assembly began to separate in the forward flange
- of the aft bulkhead.
-
- 3. The structural separation of the pylon was caused by a complete failure of
- the forward flange of the aft bulkhead after its residual strength had been
- critically reduced by the fracture and subsequent service life.
-
- 4. The overload fracture and fatigue cracking on the pylon aft bulkhead's
- upper flange were the only preexisting damage on the bulkhead. The length of
- the overload fracture and fatigue cracking was about 13 inches. The fracture
- was caused by an upward movement of the aft end of the pylon which brought the
- upper flange and its fasteners into contact with the wing clevis.
-
- 5. The pylon to wing attach hardware was properly installed at all attachment
- points.
-
- 6. All electrical power to the No. 1 AC generator bus and No. 1 DC bus was
- lost after the pylon separated. The captain's flight director instrument, the
- stall warning system, and the slat disagreement warning light systems were
- rendered inoperative. Power to these buses was never restored.
-
- 7. The No. 1 hydraulic system was lost when the pylon separated. Hydraulic
- systems No. 2 and No. 3 operated at their full capability throughout the flight.
- Except for spoiler panels No. 2 and No. 4 on each wing, all flight controls
- were operating.
-
- 8. The hydraulic lines and followup cables of the drive actuator for the left
- wing's outboard leading edge slat were severed by the separation of the pylon
- and the left wing's outboard slats retracted during climbout. The retraction
- of the slats caused an asymmetric stall and subsequent loss of control of the
- aircraft.
-
- 9. The flightcrew could not see the wings and engines from the cockpit.
- Because of the loss of the slat disagreement light and the stall warning system,
- the flightcrew would not have received an electronic warning of either the slat
- asymmetry or the stall. The loss of the warning systems created a situation
- which afforded the flightcrew an inadequate opportunity to recognize and
- prevent the ensuing stall of the aircraft.
-
- 10. The flightcrew flew the aircraft in accordance with the prescribed emer-
- gency procedure, which called for the climbout to be flown at V2 speed. V2
- was 6 KIAS below the stall speed for the left wing. The deceleration to V2
- speed caused the aircraft to stall. The start of the left roll was the only
- warning the pilot had of the onset of the stall.
-
- 11. The pylon was damaged during maintenance performed on the accident aircraft
- at American Airline's Maintenance Facility at Tulsa, Oklahoma, on March 29 and
- 30, 1979.
-
- 12. The design of the aft bulkhead made the flange vulnerable to damage when
- the pylon was being separated or attached.
-
- 13. American Airlines engineering personnel developed an ECO to remove and
- reinstall the pylon and engine as a single unit. The ECO directed that the
- combined engine and pylon assembly be supported, lowered, and raised by a
- forklift. American Airlines engineering personnel did not perform an adequate
- evaluation of either the capability of the forklift to provide the required
- precision for the task, or the degree of difficulty involved in placing the
- lift properly, or the consequences of placing the lift improperly. The CO
- did not emphasize the precision required to place the forklift properly.
-
- 14. The FAA does not approve the carriers' maintenance procedures, and a
- carrier has the right to change its maintenance procedures without FAA approval.
-
- 15. American Airlines personnel removed the aft bulkhead's bolt and bushing
- before removing the forward bulkhead attach fittings. This permitted the
- forward bulkhead to act as a pivot. Any advertent or inadvertent loss of
- forklift support to the engine and pylon assembly would produce an upward
- movement at the aft bulkhead's upper flange and bring it into contact with
- the wing clevis.
-
- 16. American Airlines maintenance personnel did not report formally to their
- maintenance engineering staff either their deviation from the removal sequence
- contained in the ECO or the difficulties they had encountered in accomplishing
- the ECO's procedures.
-
- 17. American Airline's engineering personnel did not perform a thorough
- evaluation of all aspects of the maintenance procedures before they formulated
- the ECO. The engineering and supervisory personnel did not monitor the
- performance of the ECO to ensure either that it was being accomplished properly
- or if their maintenance personnel were encountering unforeseen difficulties in
- performing the assigned tasks.
-
- 18. The nine situations in which damage was sustained and cracks were found on
- the upper flange were limited to those operations wherein the engine and pylon
- assembly was supported by a forklift.
-
- 19. On December 19, 1978, and Feb. 22, 1979, Continental Airlines maintenance
- personnel damaged aft bulkhead upper flanges in a manner similar to the damage
- noted on the accident aircraft. The carrier classified the cause of the damage
- as maintenance error. Neither the air carrier nor the manufacturer interpreted
- the regulation to require that it further investigate or reprot the damages to
- the FAA.
-
- 20. The original certification's fatigue-damage assessment was in conformance
- with the existing requirements.
-
- 21. The design of the stall warning system lacked sufficient redundancy; there
- was only one stickshaker motor; and further, the design of the system did not
- provide for crossover information to the left and right stall warning computers
- from the applicable leading edge slat sensors on the opposite side of the
- aircraft.
-
- 22. The design of the leading edge slat system did not include positive
- mechanical locking devices to prevent movement of the slats by external loads
- following a failure of the primary controls. Certification was based upon
- acceptable flight characteristics with an asymmetrical leading edge slat
- condition.
-
- 23. At the time of DC-10 certification, the structural separation of an engine
- pylon was not considered. Thus, multiple failures of other systems resulting
- from this single event was not considered.
-
-
- Additional excerpts:
-
- [design requirements for slats]
- "The motion on the flaps on opposite sides of the plane of symmetry
- must be synchronized unless the aircraft has safe characteristics with
- the flaps retracted on one side and extended on the other."
-
- Since the left and right inboard slats are controlled by a single valve and
- actuated by a common drum and the left and right outboard slats receive their
- command from mechanically linked control valves which are "slaved" to the
- inboard slats by the followup cable, the synchronization requirement was
- satisfied. However, since the cable drum actuating mechanisms of the left and
- right outboard slats were independent of each other, the possibility existed
- that one outboard slat might fail to respond to a commanded movement.
- Therefore, the safe flight characteristics of the aircraft with asymmetrical
- outboard slats were demonstrated by test flight. These flight characteristics
- were investigated within an airspeed range bounded by the limiting airspeed for
- the takeoff slat positions--260 kts--and the stall warning speed; the flight
- test did not investigate these characteristics under takeoff conditions.
- In addition, a slat disagree warning light system was installed which, when
- illuminated, indicated that the slat handle and slat position disagree, or
- the slats are in transit, or the slats have been extended automatically.
-
- The program engineer stated that the commanded slat position is held by trapped
- fluid in the actuating cylinder, and that no consideration was given to an
- alternate locking mechanism. The slats' hydraulic lines and followup cables
- were routed as close as possible to primary structure for protection; however,
- routing them behind the wing's front spar was not considered because of
- interference with other systems.
-
- "The branch chief of the Reliability and Safety Engineering Organization of the
- Douglas Aircraft Company described the failure mode and effects analysis (FMEA)
- and fault analysis. The witness indicated that the FMEA was a basic working
- document in which rational failure modes were postulated and analyzed; vendors
- and subcontractors were requested to perform similar analyses on equipment they
- supplied to McDonnell-Douglas. Previous design and service experience was
- incorporated in the initial DC-10-10's FMEA's, and analyses were modified as
- the design progressed. The FMEA's were synthesized to make fault analyses,
- which were system-oriented summary documents submitted to the FAA to satisfy 14
- CFR 25.1309. The FAA could have requested and could have reviewed the FMEA's.
-
- The basic regulations under which the slats were certified did not require
- accountability for multiple failures. The slat fault analysis submitted to the
- FAA listed 11 faults or failures, all of which were correctable by the
- flightcrew. However, one multiple failure--erroneous motion transmitted to
- the right-hand outboard slats and an engine failure on the appropriate side--
- was considered by McDonnell-Douglas in its FMEA. The FMEA noted that the
- "failure increases the amount of yaw but would be critical only under the most
- adverse flight or takeoff conditions. The probability of both failures
- occurring is less than 1 x 10e-10 [a popular number with airframe
- manufacturers!]."
-
- [...]
-
- "The December 1, 1978 revision of 14 CFR 25.571 retitled the regulation
- "Damage-Tolerance and Fatigue Evaluation of Structure." The fail-safe
- evaluation must now include damage modes due to fatigue, corrosion, and
- accidental damage. According to the manufacturer, the consideration for
- accidental damage was limited to damage which can be inflicted during routine
- maintenance and aircraft servicing."
-
- [...]
-
- "Because of the designed redundancy in the aircraft's hydraulic and electrical
- systems, the losses of those systems powered by the No. 1 engine should not have
- affected the crew's ability to control the aircraft. However, as the pylon
- separated from the aircraft, the forward bulkhead contacted and severed
- four other hydraulic lines and two cables which were routed through the wing
- leading edge forward of the bulkhead. These hydraulic lines were the operating
- lines from the leading edge slat control valve, which was located inboard of
- the pylon, and the actuating cylinders, which extend and retract the outboard
- leading edge slats. Two of the lines were connected to the No. 1 hydraulic
- system and two were connected to the No. 3 system, thus providing the
- redundancy to cope with a single hydraulic system failure. The cables which
- were severed provided feedback of the leading edge slat position so that the
- control valve would be nulled when slat position agreed with position commanded
- by the cockpit control.
-
- The severing of the hydraulic lines in the leading edge of the left wing could
- have resulted in the eventual loss of No. 3 hydraulic system because of fluid
- depletion. However, even at the most rapid rate of leakage possible, the system
- would have operated throughout the flight. The extended No. 3 spoiler panel on
- the right wing, which was operated by the No. 3 hydraulic system, confirmed that
- this hydraulic system was operating. Since two of the three hydraulic systems
- were operative, the Safety Board concludes that, except for the No. 2 and No. 4
- spoiler panels on both wings which were powered by the No. 1 hydraulic systems,
- all flight controls were operating. Therefore, except for the significant
- effect that the severing of the No. 3 hydraulic system's lines had on the left
- leading edge slat system, the fluid leak did not play a role in the accident.
-
- During takeoff, as with any normal takeoff, the leading edge slats were
- extended to provide increased aerodynamic lift on the wings . When the slats
- are extended and the control valve is nulled, hydraulic fluid is trapped in the
- actuating cylinder and operating lines. The incompressiblity of this fluid
- reacts against any external air loads and holds the slats extended. This is
- the only lock provided by the design. Thus, when the lines were severed and
- the trapped hydraulic fluid was lost, air loads forced the left outboard slats
- to retract. While other failures were not critical, the uncommanded movement
- of these leading edge slats had a profound effect on the aerodynamic performance
- and controllability of the aircraft. With the left outboard slats retracted
- and all others extended, the lift of the left wing was reduced and the airspeed
- at which that wing would stall was increased. The simulator tests showed that
- even with the loss of the No. 2 and No. 4 spoilers, sufficient lateral control
- was available from the ailerons and other spoilers to offset the asymmetric
- lift caused by left slat retraction at airspeeds above that at which the wing
- would stall. However, the stall speed for the left wing increased to 159 KIAS.
-
- [...]
-
- The Safety Board is also concerned that the designs of the flight control,
- hydraulic, and electrical systems in the DC-10 aircraft were such that all
- were affected by the pylon separation to the extent that the crew was unable to
- ascertain the measures needed to maintain control of the aircraft.
-
- The airworthiness regulations in effect when the DC-10 was certificated were
- augmented by a Special Condition, the provisions of which had to be met before
- the aircraft's fully powered control system would be certificated.
- The Special Condition required that the aircraft be capable of continued
- flight and of being landed safely after failure of the flight control system,
- including lift devices. These capabilities must be demonstrated by analysis
- or test, or both. However, the Special Condition, as it applied to the slat
- control system, was consistent with the basic airworthiness regulations in
- effect at the time. The basic airworthiness regulations specified requirements
- for wing flap asymmetry only and did not include specific consideration of
- other lift devices. Because the leading edge slat design did not contain any
- novel or unusual features, it was certificated under the basic regulation. The
- flap control requirements for symmetry and synchronization were applied to and
- satisfied by the slat system design. Since a malfunction of the slat actuating
- system could disrupt the operation of an outboard slat segment, a fault analysis
- was conducted to explore the probability and effects of both an uncommanded
- movement of the outboard slats and the failure of the outboard slats to respond
- to a commanded movement. The fault analysis concluded that the aircraft could
- be flown safely with this asymmetry.
-
- Other aircraft designs include positive mechanical locking devices to prevent
- movement of slats by external loads following a primary failure. The DC-10
- design did not include such a feature nor was it deemed necessary, since
- compliance with the regulations was based upon analysis of those failure modes
- which could result in asymmetrical positioning of the leading edge devices and
- a demonstration that sufficient lateral control was available to compensate for
- the asymmetrical conditions throughout the aircraft's flight envelope. The
- flight tests conducted to evaluate the controllability of the aircraft were
- limited to a minimum airspeed compatible with stall-warning activation
- predicated upon the slat-retracted configuration.
-
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